Removed the Wolverine power supply from the rig and added my own 12V dc adapter and a small hardwired regulator board that interfaces with the Hawkeye board. The 12V provided to the Hawkeye 3.3V regulator is too high and causing it to heat up. So decided to go with a new regulator design.
The regulator provides 5V for the Hawkeye board (will become Hawkeye2) and the 12V unregulated can be used for the stepper controller.
The regulator provides 5V for the Hawkeye board (will become Hawkeye2) and the 12V unregulated can be used for the stepper controller.
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